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Journal Articles

Technical investigation on small water leakage incident occurrence in mercury target of J-PARC

Haga, Katsuhiro; Kogawa, Hiroyuki; Wakui, Takashi; Naoe, Takashi; Takada, Hiroshi

Journal of Nuclear Science and Technology, 55(2), p.160 - 168, 2018/02

 Times Cited Count:5 Percentile:45.59(Nuclear Science & Technology)

The mercury target vessel used for the spallation neutron source in J-PARC has multi-walled structure made of stainless steel type 316L, which comprises a mercury vessel and a water shroud. In 2015, water leak incidents from the water shroud occurred while the mercury target was operated with a proton beam power of 500 kW. Several investigations were conducted to identify the cause of failure. The results of the visual inspections, mockup tests, and analytical evaluations suggested that the water leak was caused by the combination of two factors. One was the diffusion bonding failure due to the large thermal stress induced by welding of the bolt head, which fixes the mercury vessel and the water shroud, during the fabrication process. The other was the thermal fatigue failure of the seal weld due to the repetitive beam trip during the operating period. These target failures point to the importance of eliminating initial defects from welding lines and to secure the rigidity and reliability of welded structures. The next mercury target was fabricated with an improved design which adopted parts of monolithic structure machined by wire EDM to reduce welding lines, and intensified inspections to eliminate the initial defects. The operation with the improved target is planned to be started in October 2017.

JAEA Reports

The Recovery from water leakage accident in JMTR

Ito, Haruhiko; Homma, Kenzo; Itabashi, Yukio; Tabata, Toshio; Akashi, Kazutomo; Inaba, Yukio; Kumahara, Hajime; Takahashi, Kunihiro; Kitajima, Toshio; Yokouchi, Iichiro

JAERI-Review 2003-024, 76 Pages, 2003/10

JAERI-Review-2003-024.pdf:8.35MB

no abstracts in English

JAEA Reports

Report on investigation of cause of crack at instrumentation pipe in JMTR; Results of vibration and stress analysis

Hanawa, Satoshi; Tachibana, Yukio; Iyoku, Tatsuo; Ishihara, Masahiro; Ito, Haruhiko

JAERI-Tech 2003-064, 25 Pages, 2003/07

JAERI-Tech-2003-064.pdf:2.84MB

On the 147cycle operation, the water leakage was found at the pressure instrumentation pipe which is attached to the exit pipe of No.1 charge pump of the purification system of primary cooling system at JMTR in the Oarai establishment, JAERI. Then JMTR was shutted down manually on December 10th. It was predicted that the crack on the pressure instrumentation pipe was initiated and propagated by the cyclic load which was caused by the charge pump. Therefore, vibration and stress analyses of pressure instrumentation pipe were performed. From the vibration analysis, the natural frequency of the pressure instrumentation pipe of No.1 charge pump is between 53$$sim$$58Hz, which is close to the resonance frequency of 50Hz. From the stress analysis results, total stress generated on the pressure instrumentation pipe is 112.2MPa at the natural frequency of 53Hz and 74.2Mpa at 58Hz. It was found that the stress of 112.2MPa is close to the fatigue limit of used materials.

JAEA Reports

Report on investigation of cause of crack at instrumentation pipe in JMTR; Data book on examination of pressure instrumentation pipe at JMTR hot laboratory

Working Group for Investigation of Cause of Crack Initiation

JAERI-Tech 2003-060, 183 Pages, 2003/07

JAERI-Tech-2003-060.pdf:55.37MB

On December 10, 2002, the water leakage was found at the pressure instrumentation pipe attached to the exit pipe of No.1 charging pump of the purification system of a primary cooling system at JMTR, and the cracks were detected on the pressure instrumentation pipe by the visual observation. The Investigation Committee for Water Leakage from Instrumentation Pipe in JMTR was established and organized by specialists from inside and outside JAERI on December 16. In order to investigate the cause of crack initiation at the pressure instrumentation pipe, the Working Group was organized in the Department of JMTR. Visual inspection, fractgraphy test, metallographic observation and hardness test for the pressure instrumentation pipe and its weldment were carried out in the JMTR Hot Laboratory. This report summarized above data obtained by investigation on the cause of the crack initiation.

JAEA Reports

Study on core physics characteristics of high burnup full MOX PWR core, 2

Kugo, Teruhiko; Okubo, Tsutomu; *

JAERI-Research 99-057, p.29 - 0, 1999/09

JAERI-Research-99-057.pdf:1.77MB

no abstracts in English

JAEA Reports

Modification of JRR-2

JAERI-M 7484, 25 Pages, 1978/01

JAERI-M-7484.pdf:1.15MB

no abstracts in English

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